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Mini Tesla Coil 1
- 40mm
Loneoceans
/ Loneoceans Laboratories / High Voltage / Tesla Coil 1
This project was inspired by all the other tesla coils out there. Since it is my first attempt at building a tesla coil, my aims are to produce a small, relatively good-looking, working spark-gap tesla coil, more to learn about building tesla coils, and to gain invaluable experience.
This page will index my construction efforts as I update it continually during the course of my tesla coil construction. It will be updated frequently, with the most recent ones at the bottom.
Current Status: Under
Construction.. Completed! on 20th November 2003
Now under testing and tuning...
Project status halted since 2004 till further notice (28 July 2004)
Coil currently being improved. (9th August 2004)
Acknowledgements
The tesla coil is complete! I would like to thank the following people, for this coil would not have been completed without them.
- The great people at
the 4hv forums and the-geek-group forums for giving me great
advice and suggestions
- My dad and my mum who sponsored most part of the funding for
the building of this coil and for finding parts and components
together with me, and for spending time and resources, and for
tolerating the noisy coil while in operation.
- All the great tesla coils on the internet which gave me
valuable advice and construction details
- And everyone else who has helped me in one way or another.
15 Oct 2003 (Wednesday)
|
It is a F.A.R.T. brand transformer. (stands for Fabbrica Apparecchiature Radioelettriche Treviso I think.. this is living proof that a brand this name can sell so well. It is the best selling neon sign transformer in the UK by the way. www.fart.it). It's a 15kV 30mA unit, and weighs around 7+kg. The whole thing is potted in a resin block and comes with a zinc mounting plate. This design eliminates rusting and is a very sturdy transformer. Anyway, I went home and tested it. Apparently, only one secondary winding had shorted but the other half was in working condition. This makes it put out approximately 7.5kV 30mA. Just what I was looking for, for my small coil. 15kV would be a bit on the high side. Although this makes it not a very powerful unit (especially since half of it is junk and taking up extra space), it is still relatively small and delivers 225Watts with this configuration. I hope to get around 1 foot arcs from this system. However, I did not receive any High Voltage cable, so I guess I'll have to go find some... I'd probably be using this unit for my coil, unless I find another one in better condition. To test if it was working, I hooked up the mains and powered it on with half of the high voltage windings. Btttztztzzttzz! It works! At least I know that this thing can output the 7.5kV at 30mA I need. Here is the picture of the arc. 30mA is quite high (quite enough to kill!) resulting in a HOT fiery arc. I will make a large Jacob's ladder too to celebrate this find! At least I got this transformer Free. Tomorrow, I plan to buy materials for my toroidal top load... I have acquired a large roll of aluminum tape for $15. I would be constructing the top load and hopefully the spark gap (set at 8kV) tomorrow. |
18 Oct 2003 (Saturday)
|
Progress has been slow due to the un-availability of parts... until now. I have finally got most parts more construction can start. I've decided on a double toroid design, one large diameter one resting on a small diameter toriod, for better E-field shaping. Toroid The small toroid took around 2hrs to make. The small one is approximately 23 x 5.5cm. (23cm being the total diameter and 5.5cm being the pipe diameter). A commercially spun toroid would cost well over $100 new. Building this cost less than $20 and is extremely simple to make.
The first thing I did was to cut the centre disk out of some surplus plastic I had lying around. It's about a 12cm dia disk. After cutting with my saw, I drilled holes around the perimeter of the disk at roughly 1 inch intervals. These holes will hold the wire used to tie the PVC pipe to the disk. After coating the disk with aluminum tape (plumbers tape), I tied the pipe to the disk. The pipe I used is a 2" Flexible PVC drain pipe.
I just bent the twisted wire into the grooves of the corrugated PVC pipe. The pipe will automatically fit around the disk :). It's not that easy as it looks... Following that I taped the whole pipe up with masking tape, to provide a smoother finish, and finally, the aluminum tape. Basically.. it's done! I bought some nylon screws to attach it to the secondary coil. The larger coil is still needs to be wrapped with aluminum tape. Over here, flexible corrugated PVC pipe and aluminum tape don't come cheap. I thank my parents for supporting me financially :). That's it for today. I'll continue the other toroid tomorrow. It's a nice smooth toroid after smoothening it with the back of a spoon. |
19 October 2003 (Sunday)
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I completed the toroids today and fixed the spark-gap together. The spark-gap is not fully completed as I still need the fans and attach them to the gap to quench the sparks. More than 4 hours of work today.
Later in the afternoon, I got more materials and built the spark gap. It's a basic sucker-gap design, using two copper pipes as the main spark gap all housed in a plastic box with two fans to quench the arcs. I realised that those white plastic chopping boards would be much more ideal than acrylic. It costs two times cheaper for the same size (if not bigger) and is a whole lot easier to saw. I only have a lousy hand saw.. a Jig-saw would save lots of time... Here's my design.
I have a 4Amp power supply for the fans so it shouldn't be a problem even for high powered fans. At the low power my tesla coil will be running at, it shouldn't get too hot at all. It's looks easy to build, but it's not without proper cutting equipment :(. The whole gap took around 2 hours to make, except for some places which need to be covered up and another fan. The air must be forced only in between the spark gaps due to the limited amount of air flow I can get with the fans.
Looks like today has been a rather successful day. I can't do much during the weekdays due to school, so I'll have to cram more stuff during the week ends. I am now left with the filter network, capacitor bank, secondary coil, primary coil / supports... lots more work to do. I am thinking of fitting all components inside a nice box.. |
21 Oct 2003 (Tuesday)
| Not much done today. I made
a simple poor-man's rig and after drying my 40mm PVC coil
form, I varnished it with polyurethane. The set up is
basically a wooden rod through the PVC, stuck with duct tape,
and tied in between 2 chairs.
This allows me to wind the PVC as I apply the varnish. It's not as easy as it looks. Anyway, I kept rotating the pipe for about an hour with a fan blowing to allow it to set before I let it dry for the night. It's tiring.. Although it's not smooth, I'm going to fine-sand the uneven parts down before I can wind my secondary coil!
|
24 Oct 2003 (Friday)
| I completed the Primary
coil today.
I have acquired a
Black & Decker 400W jigsaw. It really saves a lot of time. The base is made of a 230x230x6mm clear acrylic surplus piece I had lying around. I made 4 supports, each with 9 spaces for the primary windings and 1 extra should a strike rail be needed to install. The stands are made out of 12mm thick white plastic chopping board material. (It's cheap and easy to get from the mart) and are attached to the base with contact cement and hot glue. The coil is made out of 3mm thick flexible copper tubing. Everything was cut and drilled by hand, and even with the help of the jigsaw, it still took around 2 hours to plan, cut and fix the mistakes. Here are some specifications: Primary Coil Inner
Diameter (from the copper tubing): 10cm
So here it is with a can for comparison. The back protective layer of the acrylic hasn't been peeled off yet, which is why it looks brown. I have attached a 40mm PVC end cap with a nylon screw to the centre of the coil to allow easier connection of the secondary coil to the primary coil. Not too bad for a beginner.. |
7th Nov 2003 (Friday)
|
Again, due to lack of parts, I was unable to continue. Yesterday, my dad helped me purchase 30 capacitors, High-Voltage rated resistors and 0.2mm enameled copper wire. I purchased acrylic and thick wires today, so work can finally begin again. Today, I completed the
primary capacitor bank using a MMC (multi mini capacitor)
setup. The capacitor is a critical element in the tesla coil.
Critical because it is really punished by the oscillations of
the Tesla tank circuit. The tank current can easily reach a
value of several hundred amperes. The RF (radio frequency)
produces intense stress on the dielectric of the cap. According to The Geek Group's capacitor design chart, the resonant cap for a 7.5kV 30mA transformer at 50hz is 0.0127uF. However, a LTR (Larger Than Resonant) Cap of a desired value of 0.0191uF(19.1nF) is recommended - LTR caps reduce the chance of over-volting the capacitor and transformer, as well as increasing the bang size and power throughput. In other words, thicker, longer sparks with less chance of damaging components. After searching, I located some nice 1.5kV 0.047uF Film-Foil Polypropylene Axial Capacitors. They have a very low loss dielectric suitable of continuous use at high AC voltages and will withstand fast rise time pulses, as well as having excellent high frequency performance, exactly what is needed for a Tesla Coil Cap.
After calculating, I acquired the above components. The 10 Mega Ohm Metal glazed High Voltage resistors are wired to each capacitor to drain off the charge after use to prevent shocks, as well as to regulated the voltages.
Here's how I wired up the capacitors. The MMC consists of 24 Capacitors, 3 strings of 8. The final value of the whole cap bank is rated at 12kV at 0.017625uF (17.6nF), close to the LTR value of 0.0191uF.
The bank was mounted on a 6mm clear acrylic sheet with a 5mm backing. I have to fix the termination connections at the end of each capacitor string. My current 40W soldering iron just can't heat the large copper cable hot enough for the solder to stick. The completed bank is visually appealing :-) and took around 3-4 hours to construct. It cost less than $40 to build - much cheaper than a few hundred dollar pulse capacitor... |
9th Nov 2003 (Sunday)
| I completed winding the
secondary coil today. My coil form is a 40mm diameter white PVC pipe. It has been dried and sealed with polyurethane varnish before winding. I have decided on a 1:6 winding ratio to add more turns in the secondary, and to allow use of slightly thicker wire (thin wire breaks too easily). I used 0.2mm wire (about AWG32?) and wound about 24cm (actually 23.6cm). With 95% fill, I get about 1100+ turns. The whole coil was wound by hand and took around 1 hour plus.
Above is the poor-man's winding setup.. I threaded a wooden dowel though the PVC form with cardboard end supports and the whole thing was kept in place with duct tape. It was then tied to a chair with wire, and was allowed to turn freely. (Okay, not so freely... ) The 0.5kg (about 1600m of wire) reel was supported by a surplus metal rod and could spin freely too. I taped the ends of the wire with duct tape.. not that nice but at least it works and sticks well. I'll just varnish over everything in the end... Winding was tiring especially for the fingers but it was all over in about an hour.
My first complete coil! It shines like a copper tube! As you can see, I've left quite a bit of extra wire at the ends. As I write this, the coil has been fully coated with polyurethane and is drying. I plan to put 4 to 5 thick coats, with fine sanding in between each coats to remove irregularities and give the coil a smoother finish. |
10th Nov 2003 (Monday)
|
On the left you can see a mock setup. Nothing is connected yet, it's just stacked up together. You can see the 15 degree inverse conical primary, the secondary coil and the double toroid configuration. The coil is meant to be pushed fully in the end caps for a quick and easy attachment. Now it somewhat balancing... The toroid is clearly not so smooth.. I have tried smoothening it out but it's not working very much. I shall see how it works out first. |
13th Nov 2003 (Thursday)
|
I made the RF ground rod today. It's a 22mm x 1' long copper tube. The wire is 3m, 6mm2 7 wire stranded PVC insulated wire and is connected to the copper tube with aluminum wire lugs with a stainless steel screw and nut. I have also made a safety spark gap consisting on threaded rods, nuts, hex end caps and a plastic container.
It's a simple but effective design, and can be easily and accurately tuned.
Almost everything is done and all I am left with is the tuning and connections! I can't wait to fire it up! |
20th Nov 2003 (Thursday)
22th Nov 2003 (Saturday)
|
It's SECOND LIGHT today! Thanks to the people at www.4hv.org (4hv forums) and www.thegeekgroup.org (geekgroup forums) for helping me debug and give suggestions to improve performance of my tesla coil. *click on pictures to enlarge. Due to long exposures, there is significant 'noise' in the photos.
Here are some changes I made: 1. Nice High Voltage
warning sign made So far, the sparkgap and safety gap is holding up fine. One design flaw I have is that the secondary height cannot be adjusted to fix coupling. Also, I did not make a portable cabinet with wheels to move it around.. However, it is quite well mounted. I am pleased with the toroids. Using only one toroid instead of two led to small arcs. If I could make changes, I would try to fix: 1. The power supply. I
believe 7.5kV at 60mA would produce much thicker arcs. My
current arcs are very thin and fine Now, the sparks. Everything is the same as run 1 except for the increase space at the sparkgap and the primary is tapped at turn 5.75 instead of 6.5 / 6 of the previous run. Second light.
The improvements have significantly improved spark length and overall, the coil is much louder.
Download Video clip of 18cm arcs:
tesla_2light.wmv (558kb) Today's maximum arc length from breakout point to RF ground : 25cm |
24th Nov 2003 (Monday)
|
Due to extremely tight schedules since the beginning of this year (2004), I am unable to do more work on this coil. More work will resume however. [ 28th July 04 ] |
|
8th August 2004
I am still not happy with the performance of my coil. After looking over my coil design, I found a possible source of problem - the spark gap. Although I believe it has great quenching power (from the powerful fan), the problem was that the copper tubes were connected to the wiring via steel wire and steel threaded rods. Steel has a high electrical resistance compared to copper or brass, and other coilers have reported instances where steel connections heated up a lot. As such, I decided to dismantle the spark gap and build a new static spark gap. In the picture you can see the eroded copper pipes. I sanded the whole pipe down so it was shiny again. The new gap will use much less copper though... And there you have it, the new adjustable static spark gap. It consists of 3 fixed copper rings screwed down to a HDPE stand. There is one adjustable brass machine screw as the last electrode. Termination electrodes are all brass. Although this can't handle as much power as the first big one, it's much smaller and this time, no steel! I'll probably add a powerful fan blowing across the gap to assist in quenching as well as to prevent it from over heating. It's probably not the nicest looking gap, but it seems to work great. In the second picture, you can see the gap firing from caps charged with my flyback. I am hoping at 225W of power, the gap won't overheat too quick though, otherwise I will have to make a new one. I'll probably build a stand to encase all the components too. Hopefully I can find more time. |
|
9th - 10th August 2004
9th August: I built a wooden stand, with 2 decks (2nd deck supported at one side and one edge, but still strong). I also cleaned up the dusty capacitor bank and changed the output lugs to thinner wire. Why thinner wire? The previous thick wire was too think and soldering was impossible. Now, although the wire is thinner, the connection is much better (soldering is possible now). When I powered the coil up, it worked for a while, then it stopped. Analysis revealed that the 15kV 30mA transformer was now fully dead! (Was half spoilt at first, so I was using the other half, 7.5kV 30mA. I'm not sure what's wrong as the whole transformer is resin potted, and thus I cannot dismantle it. Unhappy with the loss of my 225W unit, I decided to plug my dual MOT power supply supplying 12kV DC pulses to the coil. Even though I did not tune it or adjust the spark gap, there was significant arc length improvement and ground arcs were much thicker. This is evident in the photos below. I need to get a new NST to power my coil. My friend, known as raptor, happens to have a 6kV 30mA NST lying around and he is willing to trade with me it for an amount of magnet wire. Although it's only 180W this time, I have no other choice... I will be going to his house to collect it tomorrow.
Today I got the 6kV 30mA NST from my friend. The NST is the type which is in a metal container, potted with a black substance (probably tar). It's by Standard Electric Works (Hong Kong), and the date says Sep 86 on it. Though a bit rusty, it works perfectly! It's a center tapped unit. I completed the wooden stand today. The NST is the green box with a black sticker on it, and weighs around 4 - 4.5kg. I bought 4 plastic wheels (cost $5) and screwed them on the bottom to increase portability. I also built a bigger,
more durable spark gap. As you can see, there are 3 2inch long
copper pipes bolted to a HDPE board, and a 6mm brass bolt at
the end of the last pipe to make it adjustable. All
connections are now copper or brass, no more steel. I also
have a rather powerful fan blowing right on it, so quenching
should be ok. Everything including a 3A EMI filter is attached
on the stand.
On the right, you can see the coil running. Performance is ok, though I'm still unhappy with the spark length. Notice the nice streamers inside the large 300W light bulb. There is one more thing to try.. that to the increase the height of the primary to increase coupling. I hope to do that soon, and the coil will be more or less complete! |
|
13-14 August 2004
I cut out 4 6mm x 100mm x 30mm Acrylic pieces, and drilled two holes at the top 1cm. These are then tap screwed into the HDPE primary supports, effectively raising the primary coil by 2 cm to improve coupling. The hot glue and other stuff were scraped away (albeit leaving many marks on the acrylic base), and the supports were glued to it using Chloroform (trichloromethane) which is like a solvent for acrylic, allowing it to bond chemically. The second picture shows the aluminum spark gap. Also, you might have realized that I have removed the larger toroid from the coil. I tried with the small one only, and arcs seem best at turn 4.5 to 5. Streamers are now longer! (Primary would be tapped at turn 5.75 for the large one and the small one together). More test and arc photos will be taken tomorrow. I hope to improve spark length even further! |
|
14 Aug 2004 I powered up to coil today. Primary is tapped at turn 5. I did something different: Since the coil is now running inside my house (instead of in the backyard), I can't get a proper RF ground without running a very long wire. As such, I connected the bottom of the secondary winding to the first turn of the primary. This configuration is similar to an Oudin coil/resonator. Although this configuration eliminates the need for a RF ground, and also eliminates the possibility of a primary or secondary strike, it injects dangerous primary AC currents into the output streamers. Performance is most satisfactory! I guess it works without much loss in a small coil like this one. The first photo shows the coil in action with a metal rod (stuck on a wooden pole of course) drawing arcs off it. The second photo is a long exposure (a lot of digital noise) of the coil in action, and the last photo is the coil with a breakout point. The photo on the left is probably the best photo of the coil actually producing streamers. Performance has indeed increased! Note that without the larger toroid, there are even more streamers. I hypothesize that the toroid is either too small, or it is too rough. For the time being, I'll stick with this. Today's maximum arc length to ground is 25cm, and that's which 180W. Previously at 225W, maximum arc length was only 27cm. I am rather happy with the results, but I still hope to improve them. |
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21st August 2004
|
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Extremely
dangerous: Do not try at home.
I am not responsible for anything that happens should you attempt such a
project.
Last updated: 12 Aug 2004/ 28 July 2004
(c) Gao Guangyan